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가스터빈엔진 고공성능시험설비의 측정불확도 개선
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  • 가스터빈엔진 고공성능시험설비의 측정불확도 개선
저자명
이대성,양인영,전용민,김춘택,양수석,Lee. Dae-Sung,Yang. In-Young,Jun. Yong-Min,Kim. Chun-Taek,Yang. Soo-Seok
간행물명
大韓機械學會論文集. Transactions of the Korean society of mechanical engineers. B. B
권/호정보
2002년|26권 11호|pp.1496-1502 (7 pages)
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이 논문은 한국과학기술정보연구원과 논문 연계를 통해 무료로 제공되는 원문입니다.
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기타언어초록

An Altitude Engine Test Facility(AETF) was built at the Korea Aerospace Research Institute in October 1999 and has been being operated for altitude testing of gas turbine engines of 3,000 Ibf class or less. The AETF has been calibrated using several engines such as J69 of Teledyne Co. as a facility checkout engine. Uncertainty analyses on the air flow rate and thrust were performed using the test results, according to ASME PTC 19.1-1998. Several modifications on the facility and test method were made in order to improve the measurement uncertainty to a satisfactory level over the whole operating envelop. Spatial distributions of pressure and temperature were measured, sensors were substituted by more accurate ones, inlet duct was modified to refine the flow quality, and pressure control logic was revised to remove the cell pressure fluctuation. As a result, the uncertainty of the air flow measurement was improved by 0.1% over all the test conditions, and the net thrust measurement by up to 3%. The improved measurement uncertainties of air flow and thrust are 0.68~O.73% and 0.4~1.3%, respectively.